Mark SS
New Member
- Aug 7, 2020
- 4
- Boat Info
- 2008 SeaRay 240 Sundeck 5.0 MPI Bravo 3
- Engines
- 5.0 MPI Bravo #
I aquired a 2008 SeaRay Sundeck with a 5.0 MPI Bravo 3. It sat on a lift for 5 years after only a few hundred hours after the Dealer installed a brand new long block. In the time it was on the lift, it was lowered into the water and started for 10-20 minutes every few months to which it would alarm and then we would shut it off. After I acquired it finally, I went thru and put new manifolds, seawater pump, thermostat housing with all the trimmings and a new water circulation pump in addition the chipping out and cleaning the risers.
Now when I went to start it finally after all the parts and labor, I removed the blue drain plug and started it. I had it in the water and also tried the muffs and was not getting any water out of the thermostat housing drain plug hole. I shut it down and removed the inlet supply hose and found the pump was not pulling any water....followed the hose and removed the fitting on the back and, yes....Bravoitis. Going to a thru hull fitting.
Here is my question: I was getting exhaust gas thru the removed thermostat plug hole when running. I was thinking that because there was resistance with the boat in the water and the exhaust was back pressuring back thru the risers into the cooling system. Am I correct in this thinking or do I have a warped head or bad head gasket?
Now when I went to start it finally after all the parts and labor, I removed the blue drain plug and started it. I had it in the water and also tried the muffs and was not getting any water out of the thermostat housing drain plug hole. I shut it down and removed the inlet supply hose and found the pump was not pulling any water....followed the hose and removed the fitting on the back and, yes....Bravoitis. Going to a thru hull fitting.
Here is my question: I was getting exhaust gas thru the removed thermostat plug hole when running. I was thinking that because there was resistance with the boat in the water and the exhaust was back pressuring back thru the risers into the cooling system. Am I correct in this thinking or do I have a warped head or bad head gasket?